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HomeMy WebLinkAboutBAREFOOT 33N-25HZ - Well Abandonment Report - Kerr McGee - 4/4/2019Subsequent Report of Abandonment During previous workover, 7" drill bit was dropped upside-down on top of 4.5" liner hanger at 3492'. Bridge plug at 6560' has no cement Bridge plug at 3506' has no cement Unable to get past fish (drill bit) at 3491 Section Mill from 3476'-3454' with 70 sxs of cement. Cement tagged at 3078' Bridge plug at 2970 will have Bismuth on top Liners have no cement String Size of Hole Size of Casing Weight per ft Setting Depth Sacks Cement Cement Bottom Cement Top 1st Liner 6-1/8 4 1/2 11.6 12567 0 2nd Liner 6-2/7 4 1/2 11.6 6534 0 Details: If yes, explain details below If yes, explain details below Yes NoWellbore has Uncemented Casing leaks: NoYesFish in Hole: Estimated Depth:NoYesCasing to be pulled: Other Mechanical ProblemsProduction Sub-economicDryReason for Abandonment: -104.94345740.195373 Longitude: GPS Data: Only Complete the Following Background Information for Intent to Abandon Carli Sloan 1.406/16/2014 GPS Instrument Operator's Name:PDOP Reading:Date of Measurement: Latitude: 90750Field Number:Field Name:WATTENBERG Federal, Indian or State Lease Number: Meridian:668W Range:Township:3N 25Section:QtrQtr: 33N-25HZ Well Number: NESE County:WELD Location: BAREFOOTWell Name: 05-123-39230-00API Number This form is to be submitted as an Intent to Abandon whenever an abandonment is planned on a borehole. After the abandonment is complete, this form shall again be submitted as a Subsequent Report of the actual work completed. The approved intent shall be valid for six months after the approval date, after that period, a new intent will be required. Attachments required with the Intent to Abandon are wellbore diagrams of the current configuration and the proposed configuration with plugs set. A Subsequent Report of Abandonment shall indicate the actual work completed. Attachments required with a Subsequent Report are a wellbore diagram showing plugs that were set and casing remaining in the hole, the job summaries from all plugging contractors used, including wireline and cementing (third party verification) and any logs that may have been run during abandonment. State of Colorado Oil and Gas Conservation Commission 1120 Lincoln Street, Suite 801, Denver, Colorado 80203 Phone: (303) 894-2100 Fax: (303) 894-2109 WELL ABANDONMENT REPORT FORM 6 Rev 05/18 Notice of Intent to Abandon cheryl.light@anadarko.comEmail: (720) 929-7461Fax: (720) 929-6461Phone: Zip:80217- 3779 COState:DENVER P O BOX 173779 Contact Name: City: CHERYL LIGHT Address: KERR MCGEE OIL & GAS ONSHORE LPName of Operator: 47120OGCC Operator Number: craig.carlile@state.co.usEmail: Tel:(970) 629-8279Name:Carlile, Craig For "Intent" 24 hour notice required, COGCC contact: 04/04/2019 Date Received: Document Number: DE ET OE ES 401994854 Current and Previously Abandoned Zones Page 1 of 3Date Run: 5/30/2019 Doc [#401994854] Well Name: BAREFOOT 33N-25HZ *ATTACH JOB SUMMARY Technical Detail/Comments: NoYesFlowline/Pipeline has been abandoned per Rule 1105 Type of Cement and Additives Used: *Cementing Contractor: *Wireline Contractor: Plugging Date:inch casingft. of Additional Plugging Information for Subsequent Report Only Casing Recovered: Plug Tagged: Plug Type: Plug Tagged: Plug Type: Plug Tagged: Plug Type: Plug Tagged: Plug Type: Plug Tagged:CASING Plug Tagged: (Cast Iron Cement Retainer Depth) CICR Depth CICR Depth CICR Depth sacks cmt on top.withCIBP #5: Depth sacks cmt on top.withsacks cmt on top. CIPB #4: DepthwithCIBP #3: Depth Set sacks in mouse holeSetsacks in rat hole NoYesAbove Ground Dry-Hole Marker:Cut four feet below ground level, weld on plate 30Set sacks at surface ft.1685ft. to1835sacks half in. half out surface casing fromSet60 sacks. Leave at least 100 ft. in casingft. withPerforate and squeeze at sacks. Leave at least 100 ft. in casingft. withPerforate and squeeze at sacks. Leave at least 100 ft. in casing0ft. withPerforate and squeeze at 2967 ft. ft. tosks cmt fromSet ft. ft. tosks cmt fromSet ft. ft. tosks cmt fromSet ft. ft. tosks cmt fromSet ft. 2833ft. to2933sks cmt from30Set sacks cmt on top.2970 withsacks cmt on top. CIPB #2: Depth2with3050CIBP #1: Depth Plug Type: NOTE: Two(2) sacks cement required on all CIBPs. Plugging Procedure for Intent and Subsequent Report Status VISU01,735SURF 13+1/2 9+5/8 36 1,735 645 CBL1107,6261ST 8+3/4 7 26 7,626 738 1ST LINER 6+1/8 4+1/2 11.6 12,567 Casing Type Size of Hole Size of Casing Weight Per Foot Setting Depth Sacks Cement Cement TopCement Bot Casing History McCoy, Diane Formation Perf. Top Perf. Btm Abandoned Date Method of Isolation Plug Depth NIOBRARA 7660 12582 10/08/2018 B PLUG CEMENT TOP 7612 Total: 1 zone(s) Based on the information provided herein, this Well Abandonment Report (Form 6) complies with COGCC Rules and applicable orders and is hereby approved. COGCC Approved:Date:5/30/2019 I hereby certify all statements made in this form are, to the best of my knowledge, true, correct, and complete. Signed:Print Name:CHERYL LIGHT Title:Staff Regulatory Analyst Date:4/4/2019 Email:DJREGULATORY@ANADARKO.COM Page 2 of 3Date Run: 5/30/2019 Doc [#401994854] Well Name: BAREFOOT 33N-25HZ 11/29/2019Expiration Date: COA Type Description 1) Provide 48 hour notice of plugging MIRU via electronic Form 42. 2) Properly abandon flowlines per Rule 1105. File electronic Form 42 once abandonment of on-location flowlines complete. Within 30 days of an operator completing abandonment requirements for an off-location flowline or crude oil transfer line the operator must submit a Flowline Report, Form 44. 3) After pumping squeeze, shut down and shut well in at minimum 8 hours; verify gas migration has been eliminated. If evidence of gas migration or pressure remains contact COGCC Engineer for an update to plugging orders. Operator shall implement measures to control venting, to protect health and safety, and to ensure that vapors and odors from well plugging operations do not constitute a nuisance or hazard to public welfare. Prior to starting plugging operations a bradenhead test shall be performed if there has not been a reported bradenhead test within the 60 days immediately preceding the start of plugging operations. 1) If, before opening the bradenhead valve, the beginning pressure is greater than 25 psi, sampling is required. 2) If pressure remains at the conclusion of the test, or if any liquids were present during the test, sampling is required. The Form 17 shall be submitted within 10 days of the test. Sampling shall comply with Operator Guidance - Bradenhead Testing and Reporting Instructions. If samples are collected, copies of all final laboratory analytical results shall be provided to the COGCC within three (3) months of collecting the samples. Attachment Check List Att Doc Num Name 401994854 WELL ABANDONMENT REPORT (INTENT) 401994864 PROPOSED PLUGGING PROCEDURE 401994865 WELLBORE DIAGRAM 402059351 FORM 6 INTENT SUBMITTED Total Attach: 4 Files User Group Comment Comment Date Engineer Deepest water well within one mile = 50’ (17 water wells) Added first liner to casing history. Squeeze at 2967' shows zero sacks of cement, this is because operator is proposing to squeeze Bismuth at this depth. 05/30/2019 Well File Verification Pass 04/09/2019 Permit Pass 04/04/2019 Total: 3 comment(s) General Comments CONDITIONS OF APPROVAL, IF ANY: Page 3 of 3Date Run: 5/30/2019 Doc [#401994854] Well Name: BAREFOOT 33N-25HZ