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HomeMy WebLinkAboutCARMA 28-36 - Well Abandonment Report - Kerr McGee - 9/18/2018Status VISU0857SURF 12+1/4 8+5/8 24 857 540 CBL7,8948,1401ST 7+7/8 4+1/2 11.6 8,140 50 CBL3,1507,879Stage Tool 7,879 1,000 Casing Type Size of Hole Size of Casing Weight Per Foot Setting Depth Sacks Cement Cement TopCement Bot Casing History Subsequent Report of Abandonment Details: If yes, explain details below If yes, explain details below Yes NoWellbore has Uncemented Casing leaks: NoYesFish in Hole: 960Estimated Depth:NoYesCasing to be pulled: Other Mechanical ProblemsProduction Sub-economicDryReason for Abandonment: -104.94663440.187664 Longitude: GPS Data: Only Complete the Following Background Information for Intent to Abandon Renee Doiron2.409/12/2011 GPS Instrument Operator's Name:PDOP Reading:Date of Measurement: Latitude: 90750Field Number:Field Name:WATTENBERG 72/2840 Federal, Indian or State Lease Number: Meridian:668W Range:Township:3N 36Section:QtrQtr: 28-36 Well Number: NWNE County:WELD Location: CARMAWell Name: 05-123-31114-00API Number This form is to be submitted as an Intent to Abandon whenever an abandonment is planned on a borehole. After the abandonment is complete, this form shall again be submitted as a Subsequent Report of the actual work completed. The approved intent shall be valid for six months after the approval date, after that period, a new intent will be required. Attachments required with the Intent to Abandon are wellbore diagrams of the current configuration and the proposed configuration with plugs set. A Subsequent Report of Abandonment shall indicate the actual work completed. Attachments required with a Subsequent Report are a wellbore diagram showing plugs that were set and casing remaining in the hole, the job summaries from all plugging contractors used, including wireline and cementing (third party verification) and any logs that may have been run during abandonment. State of Colorado Oil and Gas Conservation Commission 1120 Lincoln Street, Suite 801, Denver, Colorado 80203 Phone: (303) 894-2100 Fax: (303) 894-2109 WELL ABANDONMENT REPORT FORM 6 Rev 05/18 Notice of Intent to Abandon cheryl.light@anadarko.comEmail: (720) 929-7461Fax: (720) 929-6461Phone: Zip:80217- 3779 COState:DENVER P O BOX 173779 Contact Name: City: CHERYL LIGHT Address: KERR MCGEE OIL & GAS ONSHORE LPName of Operator: 47120OGCC Operator Number: craig.carlile@state.co.usEmail: Tel:(970) 629-8279Name:Carlile, Craig For "Intent" 24 hour notice required, COGCC contact: 09/18/2018 Date Received: Document Number: DE ET OE ES 401766165 Formation Perf. Top Perf. Btm Abandoned Date Method of Isolation Plug Depth CODELL 7410 7428 J SAND 7842 7870 NIOBRARA 7260 7320 Total: 3 zone(s) Current and Previously Abandoned Zones Page 1 of 3Date Run: 11/15/2018 Doc [#401766165] Well Name: CARMA 28-36 *ATTACH JOB SUMMARY Technical Detail/Comments: 5/14/2019Expiration Date: NoYesFlowline/Pipeline has been abandoned per Rule 1105 Type of Cement and Additives Used: *Cementing Contractor: *Wireline Contractor: Plugging Date:inch casingft. of Additional Plugging Information for Subsequent Report Only Casing Recovered: Plug Tagged: Plug Type: Plug Tagged: Plug Type: Plug Tagged: Plug Type: Plug Tagged:CASINGPlug Type: Plug Tagged:CASING Plug Tagged: (Cast Iron Cement Retainer Depth) CICR Depth CICR Depth CICR Depth2880 sacks cmt on top.withCIBP #5: Depth sacks cmt on top.80 with 25sacks cmt on top. CIPB #4: Depth2with4010CIBP #3: Depth Set sacks in mouse holeSetsacks in rat hole NoYesAbove Ground Dry-Hole Marker:Cut four feet below ground level, weld on plate 25Set sacks at surface ft.807ft. to1060sacks half in. half out surface casing fromSet100 sacks. Leave at least 100 ft. in casingft. withPerforate and squeeze at sacks. Leave at least 100 ft. in casingft. withPerforate and squeeze at sacks. Leave at least 100 ft. in casing70ft. withPerforate and squeeze at 3120 ft. ft. tosks cmt fromSet ft. ft. tosks cmt fromSet ft. ft. tosks cmt fromSet ft. 2690ft. to2880sks cmt fromSet15 ft. 6810ft. to7160sks cmt from25Set sacks cmt on top.7160 with 25sacks cmt on top. CIPB #2: Depth2with7760CIBP #1: Depth Plug Type: NOTE: Two(2) sacks cement required on all CIBPs. Plugging Procedure for Intent and Subsequent Report McCoy, Diane Based on the information provided herein, this Well Abandonment Report (Form 6) complies with COGCC Rules and applicable orders and is hereby approved. COGCC Approved:Date:11/15/2018 I hereby certify all statements made in this form are, to the best of my knowledge, true, correct, and complete. Signed:Print Name:CHERYL LIGHT Title:Staff Regulatory Analyst Date:9/18/2018 Email:DJREGULATORY@ANADARKO.COM CONDITIONS OF APPROVAL, IF ANY: Page 2 of 3Date Run: 11/15/2018 Doc [#401766165] Well Name: CARMA 28-36 COA Type Description 1) Provide 48 hour notice of plugging MIRU via electronic Form 42. 2) Properly abandon on-location flowlines per Rule 1105. File electronic Form 42 once abandonment complete. Within 30 days of an operator completing abandonment requirements for an off-location flowline or crude oil transfer line the operator must submit a Flowline Report, Form 44. 3) Operator shall implement measures to control unnecessary and excessive venting, to protect the health and safety of the public, and to ensure that vapors and odors from well plugging operations do not constitute a nuisance or hazard to public welfare. 4) After pumping squeeze, shut down and shut well in at minimum 8 hours; verify gas migration has been eliminated. If evidence of gas migration or pressure remains contact COGCC Engineer for an update to plugging orders. Prior to starting plugging operations a bradenhead test shall be performed if there has not been a reported bradenhead test within the 60 days immediately preceding the start of plugging operations. 1) If, before opening the bradenhead valve, the beginning pressure is greater than 25 psi, sampling is required. 2) If pressure remains at the conclusion of the test, or if any liquids were present during the test, sampling is required. The Form 17 shall be submitted within 10 days of the test. Sampling shall comply with Operator Guidance - Bradenhead Testing and Reporting Instructions. If samples are collected, copies of all final laboratory analytical results shall be provided to the COGCC within three (3) months of collecting the samples. Attachment Check List Att Doc Num Name 401766165 WELL ABANDONMENT REPORT (INTENT) 401766407 PROPOSED PLUGGING PROCEDURE 401766408 WELLBORE DIAGRAM 401841010 FORM 6 INTENT SUBMITTED Total Attach: 4 Files User Group Comment Comment Date Engineer Production records indicate this well has been SI since December 2016. All shut-in wells must pass a mechanical integrity test or be plugged and abandoned within two years of the initial shut-in date, this form 6 intent does not extend that due date. DWR’s aquifer determination tool base of Laramie-Fox Hills = 111’ Deepest water well within one mile = 150’ 11/15/2018 Well File Verification Pass 09/18/2018 Total: 2 comment(s) General Comments Page 3 of 3Date Run: 11/15/2018 Doc [#401766165] Well Name: CARMA 28-36